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Post by rcdbutz on Jul 31, 2009 17:43:26 GMT -6
Kent, what happened with your G401B, it just gave up on you? It's seems to be holding pretty well for me. I just finished the build yesterday and the tail is still a little shaky, so I need to mess with the limit and delay a little bit, but overall it is a pretty solid gyro. I'm going to get one for the Blade 400, along with some better servos. Those stock ones just keep grinding gears, it's crazy.
Also, I'm noticing that the tail servo is going way beyond the range it needs to. How do I turn that part down? I have a Dx7 Tx. Learning so much by building this thing instead of going the RTF route.
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